Subsequent simulator tests showed that other DC-10 crews were unable to repeat the effort of the crew of 232. Investigators concluded that, in its damaged condition, it was not possible to land the aircraft on a runway. As a result, the crew was given much praise for managing to put the aircraft down just off the runway centerline and saving as many lives as they did.
but on the landing with only engine power for control.... that guy has some "mad skillz," holy poop, just thinking about that...wow. I assume he still had control of the ailerons and flaps, I think the different control surfaces would be on seperate hydrolic systems
but wow
It turned out that one of the passengers on board flight 232 was Dennis Fitch, a United training and check pilot with over 3,000 hours on the DC-10. Haynes asked Fitch to go back and look out the windows to check for any structural damage. When Fitch returned to the flight deck, he informed Haynes that the both of the inboard ailerons were sticking up, but none of the controls appeared to be damaged or moving.
Haynes asked Fitch to take control of the throttle levers to allow the crew time to sort out the other decisions they were facing. Fitch knelt down in front of the controls and began to work with the throttles to maintain control of the aircraft. During this time, the aircraft had completed two slow right turns while descending. Calling Sioux City approach, Haynes requested the ILS (Instrument Landing System) frequency for runway 31 (9,000ft).
The crew continued to prepare for an emergency landing, dumping fuel and extending the landing gear. A flight attendent reported that she saw damage to the aircraft's horizontal stabilizer which Dvorak went back and confirmed. The aircraft was now descending through 9,000ft some 21 miles northeast of the airport. Approach asked 232 to fly southbound to keep it east of the city and set it up for an approach to runway 31.
Fitch was unable to fight the aircraft's continuing efforts to turn right and, instead of turning southbound, the aircraft again flew a 360 which Fitch was able to stop just as the airport lay ahead of them. They were now 12 miles from the airport and lined up with the closed runway, the 6888ft. runway 22.
Fortunately, there was an open field at the far end of the runway. The controller cleared them to use the closed runway and the crew managed to get the aircraft flying straight. Unfortunately, they couldn't accurately control the airspeed and sink rate. They were descending at over 1,600 feet per minute at around 215 knots. In an incredible feat of airmanship, they managed to touch down near the beginning of the runway just off the centerline. Unfortunately, the starboard wingtip touched down just prior to the landing gear, pulling the aircraft sideways. The excess airspeed and high sink rate caused the aircraft to break up on impact, igniting into a huge fireball. Amazingly, depsite the explosion and high speed break-up, 185 people survived the accident, including all four cockpit crew members.
The plane was flown only by applying thrust to each engine to make it turn. It flew around in a downward spiral only to come in hard at over 200mph. It took three people to constantly maneuver the aircraft. Actually, there was a pilot who was a passenger who came up front to help out. Discovery ran a special on this incident. It was incredible to see the reenactment, the visual reenactment and the stories from this accident. The pilots were truly heroes in this instance.
It's great that the surviviors are doing this for the pilot and his family but I want to know how anyone can justify the cost of the operation
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